Application of Six Sigma Methodology for Enhancement of Soft Plastic Extrusion Process

The gasket manufacturing process in “Company A” faced significant challenges and inefficiencies because of high rejection rates and variation in extrusion machine, magnetic insertion machine and welding machine’s performance. All three machines were consistently generating major rejections on a dai...

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Main Authors: Muhammad Mansoor Uz Zaman Siddiqui, Adeel Tabassum
Format: Article
Language:English
Published: Universidad de Montevideo 2025-06-01
Series:Memoria Investigaciones en Ingeniería
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Online Access:http://www.revistas.um.edu.uy/index.php/ingenieria/article/view/1564
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author Muhammad Mansoor Uz Zaman Siddiqui
Adeel Tabassum
author_facet Muhammad Mansoor Uz Zaman Siddiqui
Adeel Tabassum
author_sort Muhammad Mansoor Uz Zaman Siddiqui
collection DOAJ
description The gasket manufacturing process in “Company A” faced significant challenges and inefficiencies because of high rejection rates and variation in extrusion machine, magnetic insertion machine and welding machine’s performance. All three machines were consistently generating major rejections on a daily basis including a high volume of purging rejections from the PVC soft extrusion machine, excessive trimming of oversized magnets during the magnetic insertion process, and significant rejection due to poor joint strength in the welding process of PVC profiles. In order to address these underlying issues, Six Sigma DMAIC (Define, Measure, Analyze, Improve, Control) methodology was employed in order to decrease rejection/waste, increase process efficiency and decrease defects of all three machines. The study involved process mapping, cause and effect analysis, quality function deployment (QFD) and statistical process tools such as ANOVA, regression and Cp/Cpk analysis. Root causes were identified and targeted improvements based on the data were introduced including optimized production planning, machine parameter optimization and standardization, improvement of production execution planning and storage availability, temperature controls on welding machines and encoder wheel knurling for magnetic insertion machine. The main objectives were to deal with problems including material waste, variance in magnetic strip size, issues in welding machines and frequent machine stoppages caused by improper production scheduling because of improper availability of storage space for batch production independent of door pre-assembly plan. Following implementation, results show a considerable decrease in extrusion machine rejection %age from 12% to 4.06%, a reduction in purging waste from 17 kg/day to 6.9 kg/day and an increase in machine efficiency from 50.1% to 83.3%. Furthermore, welding machine rejection %age fell from 7% to 3.7% as a result of enhanced temperature management and equipment maintenance. Size variation issue in magnet insertion machine was resolved by knurling of encoder wheel. Overall, these changes resulted in an annual cost savings of roughly 1.5 million PKR for the extrusion process and 1.2 million from magnet insertion machine. The significance of this project originates from its potential to streamline the gasket production process by reducing waste and faults while increasing machine efficiency. The results offer a replicable framework that can be employed across wide range of manufacturing industries for quality improvement and cost optimization.
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spelling doaj-art-7eaa2917896b43ad87998c765601290e2025-08-20T03:08:27ZengUniversidad de MontevideoMemoria Investigaciones en Ingeniería2301-10922301-11062025-06-012810.36561/ING.28.14Application of Six Sigma Methodology for Enhancement of Soft Plastic Extrusion ProcessMuhammad Mansoor Uz Zaman Siddiqui0https://orcid.org/0009-0007-8992-7601Adeel Tabassum1https://orcid.org/0009-0006-9375-1090NED University of Engineering and Technology, PakistánNED University of Engineering and Technology, Pakistán The gasket manufacturing process in “Company A” faced significant challenges and inefficiencies because of high rejection rates and variation in extrusion machine, magnetic insertion machine and welding machine’s performance. All three machines were consistently generating major rejections on a daily basis including a high volume of purging rejections from the PVC soft extrusion machine, excessive trimming of oversized magnets during the magnetic insertion process, and significant rejection due to poor joint strength in the welding process of PVC profiles. In order to address these underlying issues, Six Sigma DMAIC (Define, Measure, Analyze, Improve, Control) methodology was employed in order to decrease rejection/waste, increase process efficiency and decrease defects of all three machines. The study involved process mapping, cause and effect analysis, quality function deployment (QFD) and statistical process tools such as ANOVA, regression and Cp/Cpk analysis. Root causes were identified and targeted improvements based on the data were introduced including optimized production planning, machine parameter optimization and standardization, improvement of production execution planning and storage availability, temperature controls on welding machines and encoder wheel knurling for magnetic insertion machine. The main objectives were to deal with problems including material waste, variance in magnetic strip size, issues in welding machines and frequent machine stoppages caused by improper production scheduling because of improper availability of storage space for batch production independent of door pre-assembly plan. Following implementation, results show a considerable decrease in extrusion machine rejection %age from 12% to 4.06%, a reduction in purging waste from 17 kg/day to 6.9 kg/day and an increase in machine efficiency from 50.1% to 83.3%. Furthermore, welding machine rejection %age fell from 7% to 3.7% as a result of enhanced temperature management and equipment maintenance. Size variation issue in magnet insertion machine was resolved by knurling of encoder wheel. Overall, these changes resulted in an annual cost savings of roughly 1.5 million PKR for the extrusion process and 1.2 million from magnet insertion machine. The significance of this project originates from its potential to streamline the gasket production process by reducing waste and faults while increasing machine efficiency. The results offer a replicable framework that can be employed across wide range of manufacturing industries for quality improvement and cost optimization. http://www.revistas.um.edu.uy/index.php/ingenieria/article/view/1564Gasket manufacturingDMAIC methodologySix sigmaProcess optimizationwaste reductionsustainable production
spellingShingle Muhammad Mansoor Uz Zaman Siddiqui
Adeel Tabassum
Application of Six Sigma Methodology for Enhancement of Soft Plastic Extrusion Process
Memoria Investigaciones en Ingeniería
Gasket manufacturing
DMAIC methodology
Six sigma
Process optimization
waste reduction
sustainable production
title Application of Six Sigma Methodology for Enhancement of Soft Plastic Extrusion Process
title_full Application of Six Sigma Methodology for Enhancement of Soft Plastic Extrusion Process
title_fullStr Application of Six Sigma Methodology for Enhancement of Soft Plastic Extrusion Process
title_full_unstemmed Application of Six Sigma Methodology for Enhancement of Soft Plastic Extrusion Process
title_short Application of Six Sigma Methodology for Enhancement of Soft Plastic Extrusion Process
title_sort application of six sigma methodology for enhancement of soft plastic extrusion process
topic Gasket manufacturing
DMAIC methodology
Six sigma
Process optimization
waste reduction
sustainable production
url http://www.revistas.um.edu.uy/index.php/ingenieria/article/view/1564
work_keys_str_mv AT muhammadmansooruzzamansiddiqui applicationofsixsigmamethodologyforenhancementofsoftplasticextrusionprocess
AT adeeltabassum applicationofsixsigmamethodologyforenhancementofsoftplasticextrusionprocess