Analisis Ketersediaan Pasokan Listrik di PT PLN (Persero) UPK Teluk Sirih dengan Metoda Lean Six Sigma

<p>This research was conducted to analyze electricity supply availability from the steam power plant at PLN Teluk Sirih. This electricity supply availability is also called the equivalent availability factor (EAF). The regular efforts made to maintain the EAF at PLN are still corrective, by re...

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Main Authors: Muhammad Dani Gitatisna, Agus Sutanto
Format: Article
Language:English
Published: Department of Mechanical Engineering, Faculty of Engineering, Universitas Andalas 2021-04-01
Series:Metal: Jurnal Sistem Mekanik dan Termal
Subjects:
Online Access:https://metal.ft.unand.ac.id/index.php/metal/article/view/147
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author Muhammad Dani Gitatisna
Agus Sutanto
author_facet Muhammad Dani Gitatisna
Agus Sutanto
author_sort Muhammad Dani Gitatisna
collection DOAJ
description <p>This research was conducted to analyze electricity supply availability from the steam power plant at PLN Teluk Sirih. This electricity supply availability is also called the equivalent availability factor (EAF). The regular efforts made to maintain the EAF at PLN are still corrective, by repairing the damage that has occurred, and no systematic method has been implemented. Accurate analysis is required to achieve high EAF values and precision so that the problem's root cause can be resolved. This can be done by using the lean six sigma method. This method can identify waste and solve problems quickly. The methodology used is Define, Measure, Analyze, Improve, and Control (DMAIC). The waste that occurs is a defect, which is the inability of the power plant to supply electricity to customers (PLN P3BS). The identification results show that the factors that influence EAF are boiler tube leak (41.46%), DS Phase S (20.45%), equipment vibration (5.85%), bottom ash system (5.39%), and other disorders (26.84%). The EAF calculation for the last two years is 70.93%, and the six sigma level is 2.05. The improvement design is expected to eliminate boiler tube leak and increases the EAF by 6.65%. Thus, the EAF value becomes 77.85%, and the six sigma level becomes 2.26.</p>
format Article
id doaj-art-583a71da5aa44a94b9896d195677248b
institution Kabale University
issn 2598-1137
2597-4483
language English
publishDate 2021-04-01
publisher Department of Mechanical Engineering, Faculty of Engineering, Universitas Andalas
record_format Article
series Metal: Jurnal Sistem Mekanik dan Termal
spelling doaj-art-583a71da5aa44a94b9896d195677248b2025-02-01T10:20:39ZengDepartment of Mechanical Engineering, Faculty of Engineering, Universitas AndalasMetal: Jurnal Sistem Mekanik dan Termal2598-11372597-44832021-04-01511810.25077/metal.5.1.1-8.202186Analisis Ketersediaan Pasokan Listrik di PT PLN (Persero) UPK Teluk Sirih dengan Metoda Lean Six SigmaMuhammad Dani Gitatisna0Agus Sutanto1PT PLN (Persero) UPK Teluk SirihUniversitas Andalas<p>This research was conducted to analyze electricity supply availability from the steam power plant at PLN Teluk Sirih. This electricity supply availability is also called the equivalent availability factor (EAF). The regular efforts made to maintain the EAF at PLN are still corrective, by repairing the damage that has occurred, and no systematic method has been implemented. Accurate analysis is required to achieve high EAF values and precision so that the problem's root cause can be resolved. This can be done by using the lean six sigma method. This method can identify waste and solve problems quickly. The methodology used is Define, Measure, Analyze, Improve, and Control (DMAIC). The waste that occurs is a defect, which is the inability of the power plant to supply electricity to customers (PLN P3BS). The identification results show that the factors that influence EAF are boiler tube leak (41.46%), DS Phase S (20.45%), equipment vibration (5.85%), bottom ash system (5.39%), and other disorders (26.84%). The EAF calculation for the last two years is 70.93%, and the six sigma level is 2.05. The improvement design is expected to eliminate boiler tube leak and increases the EAF by 6.65%. Thus, the EAF value becomes 77.85%, and the six sigma level becomes 2.26.</p>https://metal.ft.unand.ac.id/index.php/metal/article/view/147faktor ketersediaan ekuivalen (eaf)lean six sigmapemborosanmetode dmaicpembangkit listrik tenaga uap
spellingShingle Muhammad Dani Gitatisna
Agus Sutanto
Analisis Ketersediaan Pasokan Listrik di PT PLN (Persero) UPK Teluk Sirih dengan Metoda Lean Six Sigma
Metal: Jurnal Sistem Mekanik dan Termal
faktor ketersediaan ekuivalen (eaf)
lean six sigma
pemborosan
metode dmaic
pembangkit listrik tenaga uap
title Analisis Ketersediaan Pasokan Listrik di PT PLN (Persero) UPK Teluk Sirih dengan Metoda Lean Six Sigma
title_full Analisis Ketersediaan Pasokan Listrik di PT PLN (Persero) UPK Teluk Sirih dengan Metoda Lean Six Sigma
title_fullStr Analisis Ketersediaan Pasokan Listrik di PT PLN (Persero) UPK Teluk Sirih dengan Metoda Lean Six Sigma
title_full_unstemmed Analisis Ketersediaan Pasokan Listrik di PT PLN (Persero) UPK Teluk Sirih dengan Metoda Lean Six Sigma
title_short Analisis Ketersediaan Pasokan Listrik di PT PLN (Persero) UPK Teluk Sirih dengan Metoda Lean Six Sigma
title_sort analisis ketersediaan pasokan listrik di pt pln persero upk teluk sirih dengan metoda lean six sigma
topic faktor ketersediaan ekuivalen (eaf)
lean six sigma
pemborosan
metode dmaic
pembangkit listrik tenaga uap
url https://metal.ft.unand.ac.id/index.php/metal/article/view/147
work_keys_str_mv AT muhammaddanigitatisna analisisketersediaanpasokanlistrikdiptplnperseroupkteluksirihdenganmetodaleansixsigma
AT agussutanto analisisketersediaanpasokanlistrikdiptplnperseroupkteluksirihdenganmetodaleansixsigma