Waste Reduction Analysis with Lean Manufacturing Approach
UPT Logam Yogyakarta is one of the manufacturing industries engaged in metal casting services. UPT Logam Yogyakarta has the status of a Regional Business Service Agency so that this company has the capacity to receive requests from local and foreign consumers. One of the requests produced is the pro...
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| Format: | Article |
| Language: | English |
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UIN Sunan Kalijaga, Faculty of Science and Technology, Industrial Engineering Department
2024-01-01
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| Series: | Journal of Industrial Engineering and Halal Industries |
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| Online Access: | https://ejournal.uin-suka.ac.id/saintek/JIEHIS/article/view/4218 |
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| author | Eulis Yulianti Faridah Trio Yonathan Teja Kusuma |
| author_facet | Eulis Yulianti Faridah Trio Yonathan Teja Kusuma |
| author_sort | Eulis Yulianti Faridah |
| collection | DOAJ |
| description | UPT Logam Yogyakarta is one of the manufacturing industries engaged in metal casting services. UPT Logam Yogyakarta has the status of a Regional Business Service Agency so that this company has the capacity to receive requests from local and foreign consumers. One of the requests produced is the product Panasonic Downlight NN511. The problem that occurs in this company is the waste that occurs in the production process which results in losses to the company because the production output is not optimal. This can be indicated from the capacity of the production machine in the form of a sophisticated automated die casting machine with the ability to produce a Panasonic Downlight NN511 product per 45 seconds that cannot be utilized optimally, due to an unbalanced production path caused by waste and non-value added time. As a result, the production capacity of 1040 pcs per day cannot be achieved, and is only able to produce at the rate of 200-300 pcs. As a calculation reference to determine the degree of accuracy, a adequacy and uniformity test of the data will be carried out, then calculate the rating factor and determine the allowance for the calculation of normal time and standard time. After testing and adjusting the data with the factor rating and allowance, it was found that there was a cycle time that was greater than the taktime, it explained that the metal UPT had to reduce the cycle time at the finishing and packaging stations to be able to meet customer demands. One of the large proportions of waste is the waiting time in the production process. The analysis to determine the root cause of the problem is carried out using a fishbone diagram. To optimize available resources and increase production efficiency, several continuous improvements are needed in the flow pattern of the Panasonic Downlight NN511 production process. balancing, compiling the layout using Activity Relationships Chart, and collapsing diagrams. From these improvements, it is hoped that Yogyakarta Metals UPT in producing the Panasonic Downlight NN511 can achieve a higher level of productivity. |
| format | Article |
| id | doaj-art-514be7ababa64029a130ece3e642caf7 |
| institution | DOAJ |
| issn | 2722-8150 2722-8142 |
| language | English |
| publishDate | 2024-01-01 |
| publisher | UIN Sunan Kalijaga, Faculty of Science and Technology, Industrial Engineering Department |
| record_format | Article |
| series | Journal of Industrial Engineering and Halal Industries |
| spelling | doaj-art-514be7ababa64029a130ece3e642caf72025-08-20T03:15:04ZengUIN Sunan Kalijaga, Faculty of Science and Technology, Industrial Engineering DepartmentJournal of Industrial Engineering and Halal Industries2722-81502722-81422024-01-0142738410.14421/jiehis.42183842Waste Reduction Analysis with Lean Manufacturing ApproachEulis Yulianti Faridah0Trio Yonathan Teja Kusuma1UIN Sunan Kalijaga YogyakartaUIN Sunan Kalijaga YogyakartaUPT Logam Yogyakarta is one of the manufacturing industries engaged in metal casting services. UPT Logam Yogyakarta has the status of a Regional Business Service Agency so that this company has the capacity to receive requests from local and foreign consumers. One of the requests produced is the product Panasonic Downlight NN511. The problem that occurs in this company is the waste that occurs in the production process which results in losses to the company because the production output is not optimal. This can be indicated from the capacity of the production machine in the form of a sophisticated automated die casting machine with the ability to produce a Panasonic Downlight NN511 product per 45 seconds that cannot be utilized optimally, due to an unbalanced production path caused by waste and non-value added time. As a result, the production capacity of 1040 pcs per day cannot be achieved, and is only able to produce at the rate of 200-300 pcs. As a calculation reference to determine the degree of accuracy, a adequacy and uniformity test of the data will be carried out, then calculate the rating factor and determine the allowance for the calculation of normal time and standard time. After testing and adjusting the data with the factor rating and allowance, it was found that there was a cycle time that was greater than the taktime, it explained that the metal UPT had to reduce the cycle time at the finishing and packaging stations to be able to meet customer demands. One of the large proportions of waste is the waiting time in the production process. The analysis to determine the root cause of the problem is carried out using a fishbone diagram. To optimize available resources and increase production efficiency, several continuous improvements are needed in the flow pattern of the Panasonic Downlight NN511 production process. balancing, compiling the layout using Activity Relationships Chart, and collapsing diagrams. From these improvements, it is hoped that Yogyakarta Metals UPT in producing the Panasonic Downlight NN511 can achieve a higher level of productivity.https://ejournal.uin-suka.ac.id/saintek/JIEHIS/article/view/4218normal timestandard timecycle timetakt timefishbone diagramvalue stream mappingvalsatline balancingactivity relationships chartdiagram corlap |
| spellingShingle | Eulis Yulianti Faridah Trio Yonathan Teja Kusuma Waste Reduction Analysis with Lean Manufacturing Approach Journal of Industrial Engineering and Halal Industries normal time standard time cycle time takt time fishbone diagram value stream mapping valsat line balancing activity relationships chart diagram corlap |
| title | Waste Reduction Analysis with Lean Manufacturing Approach |
| title_full | Waste Reduction Analysis with Lean Manufacturing Approach |
| title_fullStr | Waste Reduction Analysis with Lean Manufacturing Approach |
| title_full_unstemmed | Waste Reduction Analysis with Lean Manufacturing Approach |
| title_short | Waste Reduction Analysis with Lean Manufacturing Approach |
| title_sort | waste reduction analysis with lean manufacturing approach |
| topic | normal time standard time cycle time takt time fishbone diagram value stream mapping valsat line balancing activity relationships chart diagram corlap |
| url | https://ejournal.uin-suka.ac.id/saintek/JIEHIS/article/view/4218 |
| work_keys_str_mv | AT eulisyuliantifaridah wastereductionanalysiswithleanmanufacturingapproach AT trioyonathantejakusuma wastereductionanalysiswithleanmanufacturingapproach |