Development of an individual warp beam tension control system for warp assembling machines in direct warp preparation
Warp preparation is a process prior to weaving that brings all the ends side by side and then winding them on a warp beam with the same tension and length at a predetermined width, density and length. Modern warp preparation machines employ feedback control systems controlling total or individual wa...
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Format: | Article |
Language: | English |
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SAGE Publishing
2025-02-01
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Series: | Journal of Engineered Fibers and Fabrics |
Online Access: | https://doi.org/10.1177/15589250251313609 |
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author | Recep Eren Sinan Kılıç Ömer Atalay |
author_facet | Recep Eren Sinan Kılıç Ömer Atalay |
author_sort | Recep Eren |
collection | DOAJ |
description | Warp preparation is a process prior to weaving that brings all the ends side by side and then winding them on a warp beam with the same tension and length at a predetermined width, density and length. Modern warp preparation machines employ feedback control systems controlling total or individual warp tension. Older warping machines in industry mostly do not have a precise feedback tension control systems and do not match with the quality requirements of today’s market expectations. This paper presents a research in which an individual section beam warp tension control system is explained for converting older beam-assembling machines to a new technology in a direct warping process. The total warp tension of each section warp beam was measured and breaking torque of the magnetic powder brake was adjusted when a deviation occured from the set tension value. It was shown that average loom efficiency increased by 5.65% despite an increase in average loom speed from 663 to 733 rpm in an air jet loom factory. The fabric fault ratio decreased from 3.45% to 1.04% per 100 m of fabric and warp waste decreased from 0.5% to below 0.2% with the new individual section warp beam tension control system adapted to an older version of the assembling machine having total tension control and section warp beam pneumatic brake system. |
format | Article |
id | doaj-art-4e3ccd84ff2844a680c570505a41e8ac |
institution | Kabale University |
issn | 1558-9250 |
language | English |
publishDate | 2025-02-01 |
publisher | SAGE Publishing |
record_format | Article |
series | Journal of Engineered Fibers and Fabrics |
spelling | doaj-art-4e3ccd84ff2844a680c570505a41e8ac2025-02-05T13:03:52ZengSAGE PublishingJournal of Engineered Fibers and Fabrics1558-92502025-02-012010.1177/15589250251313609Development of an individual warp beam tension control system for warp assembling machines in direct warp preparationRecep Eren0Sinan Kılıç1Ömer Atalay2Engineering Faculty, Textile Engineering Department, Bursa Uludag University, Nilüfer, Bursa, TürkiyeKARESI POLYESTER VE PETROKIMYA SANAYI A.Ş., R&D Center, Gürsu, Bursa, TürkiyeKARESI POLYESTER VE PETROKIMYA SANAYI A.Ş., R&D Center, Gürsu, Bursa, TürkiyeWarp preparation is a process prior to weaving that brings all the ends side by side and then winding them on a warp beam with the same tension and length at a predetermined width, density and length. Modern warp preparation machines employ feedback control systems controlling total or individual warp tension. Older warping machines in industry mostly do not have a precise feedback tension control systems and do not match with the quality requirements of today’s market expectations. This paper presents a research in which an individual section beam warp tension control system is explained for converting older beam-assembling machines to a new technology in a direct warping process. The total warp tension of each section warp beam was measured and breaking torque of the magnetic powder brake was adjusted when a deviation occured from the set tension value. It was shown that average loom efficiency increased by 5.65% despite an increase in average loom speed from 663 to 733 rpm in an air jet loom factory. The fabric fault ratio decreased from 3.45% to 1.04% per 100 m of fabric and warp waste decreased from 0.5% to below 0.2% with the new individual section warp beam tension control system adapted to an older version of the assembling machine having total tension control and section warp beam pneumatic brake system.https://doi.org/10.1177/15589250251313609 |
spellingShingle | Recep Eren Sinan Kılıç Ömer Atalay Development of an individual warp beam tension control system for warp assembling machines in direct warp preparation Journal of Engineered Fibers and Fabrics |
title | Development of an individual warp beam tension control system for warp assembling machines in direct warp preparation |
title_full | Development of an individual warp beam tension control system for warp assembling machines in direct warp preparation |
title_fullStr | Development of an individual warp beam tension control system for warp assembling machines in direct warp preparation |
title_full_unstemmed | Development of an individual warp beam tension control system for warp assembling machines in direct warp preparation |
title_short | Development of an individual warp beam tension control system for warp assembling machines in direct warp preparation |
title_sort | development of an individual warp beam tension control system for warp assembling machines in direct warp preparation |
url | https://doi.org/10.1177/15589250251313609 |
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