Numerical Study on the Flow Mechanism of Compressor Rotor Blade Vibration under Different Inlet Probe Configurations
In the performance test of a compressor, the overstrain alarm of a rotor blade occurred and it was thought to be caused by a large-sized inlet probe. To explain and further avoid the occurrence of this phenomenon, the influences of probe strut configuration on the vibration strain of the compressor...
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| Main Authors: | Rongfei Yang, Guoliang Wang, Haixu Liu, Honghui Xiang, Jie Gao |
|---|---|
| Format: | Article |
| Language: | English |
| Published: |
Wiley
2020-01-01
|
| Series: | International Journal of Aerospace Engineering |
| Online Access: | http://dx.doi.org/10.1155/2020/8897211 |
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