Optimizing Recycled Tunnel Boring Machine (TBM)-Excavated Materials as Aggregates in Shotcrete Mix Design

Tunnel Boring Machine (TBM) excavation materials were recycled by sieving and separating particles into sizes 5–10 mm (coarse aggregates) and below 5 mm (manufactured sand) to explore their potential as aggregates in shotcrete production, with the aim of reducing environmental harm from waste dispos...

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Bibliographic Details
Main Authors: Wei Zhang, Rusheng Hao, Zhijun Men, Jingjing He, Yong Zhang, Wei Hu
Format: Article
Language:English
Published: MDPI AG 2025-04-01
Series:Buildings
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Online Access:https://www.mdpi.com/2075-5309/15/9/1483
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Summary:Tunnel Boring Machine (TBM) excavation materials were recycled by sieving and separating particles into sizes 5–10 mm (coarse aggregates) and below 5 mm (manufactured sand) to explore their potential as aggregates in shotcrete production, with the aim of reducing environmental harm from waste disposal. Mix proportion experiments were conducted to evaluate the mechanical properties—including failure patterns, compressive strength, flexural strength, and deflection—of the shotcrete specimens through cubic axial compression and four-point bending tests; furthermore, rebound tests were conducted on shotcrete mixed with the recycled TBM aggregates in foundation pit engineering. These tests assessed the effects of key parameters (water–binder ratio, sand ratio, fly ash content, synthetic fibers, and liquid alkali-free accelerator) on shotcrete composed of recycled TBM sand and gravel. The results indicated that crushing and grading flaky TBM-excavated rock fragments, and subsequently blending them with pre-screened fine aggregates in a 4:1 ratio, yielded manufactured sand with an optimized particle gradation and controlled stone powder content (18%). Adjusting the water–binder ratio (0.4–0.5), fly ash dosage (mixed with 0–20%), and sand ratio (0.5–0.6) are feasible steps in preparing shotcrete with a compressive strength of 29.1 MPa to 50.4 MPa and slump of 9 cm to 20 cm. Moreover, the rebound rate of the shotcrete reached 11.3% by applying polyoxymethylene (POM) fibers with a 0.15% volume fraction and a liquid-state alkali-free setting accelerator (8% dosage), demonstrating that the implemented approach enables a decrease in the rebound rate of shotcrete.
ISSN:2075-5309