机械夹持手的优化设计与分析
Taking the injection molding machine robot gripper as example,the 3D solid model design is carried out under the environment of SolidWorks.The model is led into ANSYS Workbench, the static analysis of gripper is carried out.The structure is improved by using topology optimization module of Workbench...
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| Format: | Article |
| Language: | zho |
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Editorial Office of Journal of Mechanical Transmission
2014-01-01
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| Series: | Jixie chuandong |
| Online Access: | http://www.jxcd.net.cn/thesisDetails#10.16578/j.issn.1004.2539.2014.03.041 |
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| _version_ | 1850154326860759040 |
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| author | 郑国穗 卢军 马金锋 |
| author_facet | 郑国穗 卢军 马金锋 |
| author_sort | 郑国穗 |
| collection | DOAJ |
| description | Taking the injection molding machine robot gripper as example,the 3D solid model design is carried out under the environment of SolidWorks.The model is led into ANSYS Workbench, the static analysis of gripper is carried out.The structure is improved by using topology optimization module of Workbench,the deformation amount of the structure is greatly reduced and the weight of the optimized structure is reduced by 4.59kg,the result proved the rationality and feasibility of this program,and the reference and basis for further improvement and design is provided. |
| format | Article |
| id | doaj-art-0c9f3d03bf99481eb10cf338f7e89658 |
| institution | OA Journals |
| issn | 1004-2539 |
| language | zho |
| publishDate | 2014-01-01 |
| publisher | Editorial Office of Journal of Mechanical Transmission |
| record_format | Article |
| series | Jixie chuandong |
| spelling | doaj-art-0c9f3d03bf99481eb10cf338f7e896582025-08-20T02:25:24ZzhoEditorial Office of Journal of Mechanical TransmissionJixie chuandong1004-25392014-01-01389810188641995机械夹持手的优化设计与分析郑国穗卢军马金锋Taking the injection molding machine robot gripper as example,the 3D solid model design is carried out under the environment of SolidWorks.The model is led into ANSYS Workbench, the static analysis of gripper is carried out.The structure is improved by using topology optimization module of Workbench,the deformation amount of the structure is greatly reduced and the weight of the optimized structure is reduced by 4.59kg,the result proved the rationality and feasibility of this program,and the reference and basis for further improvement and design is provided.http://www.jxcd.net.cn/thesisDetails#10.16578/j.issn.1004.2539.2014.03.041 |
| spellingShingle | 郑国穗 卢军 马金锋 机械夹持手的优化设计与分析 Jixie chuandong |
| title | 机械夹持手的优化设计与分析 |
| title_full | 机械夹持手的优化设计与分析 |
| title_fullStr | 机械夹持手的优化设计与分析 |
| title_full_unstemmed | 机械夹持手的优化设计与分析 |
| title_short | 机械夹持手的优化设计与分析 |
| title_sort | 机械夹持手的优化设计与分析 |
| url | http://www.jxcd.net.cn/thesisDetails#10.16578/j.issn.1004.2539.2014.03.041 |
| work_keys_str_mv | AT zhèngguósuì jīxièjiāchíshǒudeyōuhuàshèjìyǔfēnxī AT lújūn jīxièjiāchíshǒudeyōuhuàshèjìyǔfēnxī AT mǎjīnfēng jīxièjiāchíshǒudeyōuhuàshèjìyǔfēnxī |